Codes

2nd Lt. John J. Flanigan

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John J. Flanigan Crew with Royal Flush (left to right)
Standing: Earl Richardson, John (Jack "Skippy) Flanigan, Douglas Dunsdon,
and Rudolph Grum
Kneeling: Salvatore J. Luistro, Frederick "Farmer" Brown, Guy M. Tuccero,
Jack J.  Strang, Adam  "Rudy" Rutkowski, Guerino "Bill" Melchiorre
100th BG Photo Archives
 
 
John J. Flanigan Crew (Flight and Ground)
William Groenendaal is middle row, far left.
100th BG Photo Archives
 

The John J. Flanigan Crew
In this photo, Carl Platkin flew as a spare gunner.  He is standing 2nd from Right.
Photo courtesy of David Platkin, son of Carl Platkin
 
2nd Lt. John J. Flanigan P CPT ?/2/44 Taps 1976
2nd Lt. Douglas E. Dunsdon CP CPT -- --
2nd Lt. Earl L. Richardson BOM POW 6/3/44 (with David Miner)
2nd Lt. Rudolph Grum NAV POW 10/10/43 (with John F. Stephens)
T/Sgt. Guy M. Tuccero TTE CPT -- --
S/Sgt. Adam E. Rutkowski ROG CPT -- --
S/Sgt. Guerino Melchiorre BTG CPT -- --
S/Sgt. Frederick D. Brown WG CPT -- --
Pvt. Salvatore J. Luistro WG CPT -- --
S/Sgt. Jack J. Strang TG CPT -- --

Crew joined the 100th BG (418th Sqdn.) 3/9/43. Crew flew in "Royal Flush" for 19 missions.

Info from the report of Paddleboat's Proxy as told by Capt. Elton
(Thanks to Jeff DeLong for this information):
I took off at 1833, September 6, 1943 to slow time a new engine (no. 3). The others aboard were 910 Pilot and Co-Pilot of a replacement crew. (2) Our squadron line chief (engineering). At 1925 I attempted to contact the tower for landing instruction and found my radio out. I then attempted to get visual (green light) by flying over the field gear down. The right gear would not extend either electrically or manually. As darkness was approaching I knew that I had to set it down shortly, regardless of the full gas load (approximately 1600 Gallons.) I fired a red-red flare on those dry run approaches and dropped a note to the man on the tower. When I sure that all on the ground was ready, ambulances, fire-truck, and men in asbestos suits, I landed the ship on the grass paralleling our E-W runway. Nothing unusual happened.

John B. Kidd added the following:
A report from the squadron engineering officer stated that the upper limit switch failed to operate causing the motor to burn out, and the clutch to freeze. This prevented the gear from being lowered by the hand crank. No responsibility can be placed upon the crew due to the mechanical nature of the failure. I witnessed the landing, which was excellent.

The report listed J. J. Flanigan (CP), G. A. VanGemert (E), and D. E. Dunsdon (CP) as the other crew members with Capt. Elton. It also stated that the aircraft was recovered by the 98th Service Squadron. The accident happened Sept. 6, 43 and the report was stamped as received by Headquarters Flight Control Command in Winston-Salem, NC on Oct. 2, 43. The report totaled 9 pages.

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