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Original 100th - Page 3

by James R. Brown

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Crew #4 -- Aircraft #4230035 -- "Torchy"
1st Lt Sam L. Barr P CPT 14-Jan-44 --
F/O Dan Barna CP POW 10-Oct-43 Munster (With Crew #7)
2nd Lt James R. Brown N SWA 15-Sep-43 Paris
2nd Lt Howard J. Kelly B CPT 30-Jan-44 --
T/Sgt Robert E. Cliff E CPT 21-Jan-44 --
S/Sgt William Ohl WG CPT -- --
T/Sgt Michael J. Tanowigch R KIA 6-Mar-44 Berlin
S/Sgt Max Russ BT CPT 21-Jan-44 --
S/Sgt Hobart Spires WG KIA 6-Mar-44 Berlin
S/Sgt James T. Hiten TG CPT 21-Jan-44 --

The composition of this crew, lead crew of the 349th, was to change considerably in the six months following its first mission of 25 June 1943. After a few missions, Joe Kelly had an extended period of illness during which he was replaced by "Big Joe" Armanini from Crew #8. This writer was severely wounded on a milk run to Paris (my life was saved by Anmanini's prompt, effective, but damn clumsy first aid) and that was the last mission I flew. Howard Bassett from Crew #8 replaced me as navigator. Dan Barna went to Crew #7 and was with that crew on the terrible Munster mission.

Mike Tanowigch and Hobart Spires finally made it to Berlin (with other crews) but their luck ran out and they did not make it back.

Everyone knows the story of Sammy Barr, the stocky, lionhearted Mississippian. Utterly fearless and grimly determined, Sam continued to fly combat missions long after he could have stopped. After becoming Squadron commander of the 349th, he continued until he had 50 missions to his credit  second only to Robert Rosenthal's 52.

One of the most loved and respected flyers of the 100th, Sam continued with the Air Force after WW II  saw active service in Korea  and finally retired as a Colonel about ten years ago. Although suffering a partial loss of speech and some paralysis, the aftermath of a severe stroke, Sam continues life with the same imdomitable spirit he shower during his career with Eighth A.F.

The planes flown by this crew: Torchy, Torchy 2nd, and Torchy 3rd, were named after the redheaded wife of this writer whom all the crew had come to know when she stayed briefly at Sioux City, Pierre, South Dakota, and Kearney, Nebraska. Torchy 3rd came to her end in April 1944 when ditched in the English Channel by a crew piloted by James Stout.
 

Crew #5 -- Aircraft #4230002 -- "Damdifino" -- M.A.C.R. #682
1st Lt Glen S. Van Noy P POW 17-Aug-43 Regensburg
2nd Lt James B. Evans CP POW 17-Aug-43 Regensburg
1st Lt Kenneth G. Allen NAV POW 17-Aug-43 Regensburg
2nd Lt William H. Couch BOM POW 17-Aug-43 Regensburg
T/Sgt William R. Stewart TTE POW 17-Aug-43 Regensburg
Col William L. Kennedy RWG POW 17-Aug-43 Regensburg
S/Sgt George P. Gineikis RWG EVA 5-Nov-43 Gelsenkirchen
T/Sgt William W. Crabb LWG POW 17-Aug-43 Regensburg
S/Sgt James D. Gibson ROG POW 17-Aug-43 Regensburg
S/Sgt Joe F. Hruskocy BTG POW 17-Aug-43 Regensburg
S/Sgt Samuel J. Cusmano TG POW 17-Aug-43 Regensburg

On the Regensburg mission this crew was leading the second element of the 349th squadron, which, led by Veal and Barr, was the high squadron. Their aircraft this day was #4230042, "Oh Nausea". About an hour before takeoff, a Colonel William L. Kennedy had replaced George Gineikis as a waist gunner. Kennedy was an armorer and gunnery expert who was soon to return to the U.S. and, before his return, wanted to get some firsthand experience as to exactly what problems our gunners were facing in combat. Of Kennedy, Bill Crab was later to say, "He kept squeezing off one round at a time and I remember thinking, 'My God! a short burst is one thing but this is ridiculous."' The Colonel became a POW with the rest of the crew.

Soon after crossing the enemy coast, a fighter pass knocked out one engine and at the target a second engine was lost. Under almost constant attack, Crabb (in the ball turret this day) ran out of ammo before reaching Regensburg although he had started the mission with 1100 rounds for one gun and 900 for the other. Realizing that they probably could not reach Africa, the decision was made to try for Sicily which, according to the morning briefing, was supposed to fall to the Allies that day. It did.

One bomb had hung up over the target and Couch tried to release it over a small airfield near the Brenner pass but it wouldn't go. Later it was released manually over the Mediterranean. Van Noy went down to about 500 feet and the crew began to throw out everything detachable to lighten the ship. Eeven shoes were discarded. Such efforts were of no avail however for a third engine went out about 90 miles north of Sicily and Van Noy and Evans made a perfect landing on the deep blue sea. One crew member was to say, "Van Noy never could land an airplane except when it really counted."

The crew got into the two five man dinghies and a smaller one with "lots of rations, radio, etc." "Oh Nausea" floated about an hour and a half before she finally sank and the crew was picked up by Germans in a flying boat the next morning.

Bill Couch probably had the biggest feet in the Eighth A.F. and one of the Germans, noticing the shoeless Couch, remarked that, "No shoes in Italy will fit that man."

On 28 June 1943, Crew #5 had nearly had it's luck run out when, during the mission to St. Nazaire, one engine was disabled. Van Noy, unable to maintain formation, had gone down to the deck and flew back to England at an average altitude of 50 feet.
 

Crew #6 -- Aircraft #423229
1st Lt Woodrow B. Barnhill P KIC 16-Jul-43 Thorpe Abbotts
2nd Lt Carl F. Hudson CP KIC 16-Jul-43 Thorpe Abbotts
2nd Lt William H. Carr N KIC 16-Jul-43 Thorpe Abbotts
1st Lt Winifred L: Rucker B KIC 16-Jul-43 Thorpe Abbotts
T/Sgt Peter Contos E KIC 16-Jul-43 Thorpe Abbotts
S/Sgt Newton E. Harris, Jr. WG KIC 16-Jul-43 Thorpe Abbotts
T/Sgt Edward D. Johnson R KIC 16-Jul-43 Thorpe Abbotts
Sgt Frank M. Opala BT IIC 16-Jul-43 Thorpe Abbotts
S/Sgt Vincent S. Noel WG IIC 16-Jul-43 Thorpe Abbotts
S/Sgt Peter S. Russell, Jr. TG IIC 16-Jul-43 Thorpe Abbotts

On 16 July 1943, this crew took off on a practice mission but crashed near the rectory at Dickleburgh a moment or two after taking off. The official report of the crash reads as follows:

"On 16 July 1943, B17F, serial number 4230305, took off from Station #139 on a local formation practice mission. Weather was clear and visibility unlimited. Takeoff was at 1006 local time. After takeoff, the aircraft entered a right bank almost immediately. The bank continued, and the aircraft lost altitude until ground impact. Duration of the flight did not exceed 30 seconds. Three crew embers in the rear of the aircraft survived with injuries. The other seven crew members received fatal injuries, and the aircraft was destroyed."

Ken Everett, who has been most active in the efforts to restore the Control Tower at Thorpe Abbotts and who now lives near the tower, was a 12yearold at the time of this crash but remembers it vividly. He says, "I recall the plane passing overhead very low and then hitting trees about 200 yards away. The dead were buried at the U.S. cemetery at Madingly near Cambridge."

In a letter to this writer dated 30 November 1978, Vince Noel stated as follows: "Peter Russell and I did survive the crash and fire but, due to our severe injuries, we were removed from flying status. At my request I was permitted to remain with the 349th until June 1945 and then returned to the U.S." Noel made no mention as to what happened to Frank Opala, the third injured man.

Loss of this crew coupled with the loss of three others  four crews in three weeks  plunged the squadron into bitter gloom.
 

Crew #7 -- Aircraft #42 30042 -- "Oh Nausea" -- M.A.C.R.#1020
1st Lt Magee C. Fuller P POW 20-Jul-44 Merseburg
2nd Lt Winton L. MacCarter CP POW 10-Oct-43 Munster
2nd Lt Harold L. Weachter N POW 10-Oct-43 Munster
2nd Lt George H. Ziegler B POW 10-Oct-43 Munster
T/Sgt Jack C. Rogers E POW 10-Oct-43 Munster
S/Sgt Robert W. Sandy R POW 10-Oct-43 Munster
S/Sgt Alexander F. Sawicki BT POW 10-Oct-43 Munster
S/Sgt Cosimo A. DeMonica WG POW 10-Oct-43 Munster
S/Sgt Raymond J. Manley TG POW 10-Oct-43 Munster
S/Sgt George W. Easterwed WG -- 01-Jul-43 GROUNDED

After a few missions, Magee Fuller was made operations officer of the 349th and was later transferred to the 418th where he became Squadron Commander. Magee appears to be the last of the original air crewmen of the 100th to be lost to enemy action.

When Fuller left the crew, MacCarter became first pilot and Dan Barna roved over from Crew #4 to become copilot. George Easterwed was grounded for some reason soon after the group arrived in England and his place on the crew was filled by S/Sgt. Roy B. Graff, a Minnesota boy from a Provisional Group. Both Barna and Graff became POWs on the Munster mission.

On the terrible Munster mission, Aircraft #4230090, "El P'sstofo", was swarmed by fighters and #1 engine began to burn. The fire quickly spread to the left wing and gas tank. The entire crew bailed out successfully and were immediately taken prisoner. The enlisted men spent the remainder of the war in Stalag 17B, Krems, Austria.

In 1973, one of Ray Manley's sons graduated from the Air Force Academy. Perhaps the Air Force fever continues from generation to generation.

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